It’s amazing how quickly things end up coming together in the end. After spending as much time as I could on The 110 recently it has got to the point where I am easily putting things back together surging head long towards getting an MOT put on it.
With that in mind I decided that I was getting a little fed up with falling through the gaps where the floor should be whilst clambering over two seats that moved around more than my teenage daughter.
So the first point of call was to get those seats secured for now. They will be coming out again once the motor is on the road to soundproof it better but for now I am happy to keep it nice and functional, just how it was originally designed.
I soon made short work of popping the main tunnel and floor pans back into place. These for now are just resting there incase I need a little better access to the gearbox or transfer box whilst getting the final set ups sorted out.
A freshly charged battery was grabbed from the garage, fitted and secured into the recently welded up battery box.
The exhaust was now fitted so with no fear of being gassed once again I climbed into the drivers seat and turned the key in the ignition to be met by the 200tdi engine bursting into more or less instantaneous life. This was accompanied by the usual grin from me but now was the moment of truth seeing if everything I had refitted would work making the car once again move under it’s own steam.
I dipped the clutch pedal that gave enough satisfying resistance then gently tried to engage reverse gear. It slotted perfectly and smoothly into place. I let the clutch pedal up a little and was soon met by the biting point. I grinned like a nut case once again and let the clutch gently start to bite and the whole 110 began to move slowly backwards along the drive.
To say I was preoccupied in my amazement that I had actually put everything back together correctly would be an understatement and only just in time did I realise that I was about to reverse into the fence that The 110 had been tightly parked up against! In fact I am not sure how I managed to move the fifteen back that I did without bumping into the fence already.
This though gave me the opportunity to see if it would move forward as well as backwards so I selected first gear and smoothly drove forwards with no issues.
I soon had it all the way up and off of the driveway as far from the house as I could to let it tick over warming itself through for the first time in years just incase something went bang or caught fire.
To say I was happy is an understatement. My creation has proved itself by moving at least fifty feet under it’s own steam! Yes it smelt a little burning oily but I just put this down to it being sitting around for years along with the odd spillage here and there when I changed all of the fluids before firing it up.
Nothing to worry about.
Well nothing for about five minutes until I noticed the alarming amount of oil that was dripping out of the Turbo itself…
I literally hopped back into the drivers seat, drove it over the hump of the driveway then killed the ignition letting gravity on my downhill driveway pull The 110 back into it’s semi dry working spot under the car port.
I felt really disappointed. Talk about one step forwards then two steps back. Add to that I am skint and it will take me several months to save up for a replacement turbo I could have cried a little. I was literally ready to throw in the towel proper then, just sell the whole damned thing and buy myself a facelift Discovery 2 instead because at least then I would have something I could use straight away.
Time for a cup of tea then.
Twenty minutes out had seen me take a few deep breaths, go back to this expense peice of scrap I owned and refit the drivers side wing. I wanted to offer up most of the front end because the radiators seemed to be sitting a little high for the bonnet. I was right there too. I need to adjust the mounting brackets lowering them by about 30mm so that the bonnet will actually close.
I also had to trim the outer brackets off of the radiator cage as well as these were fouling the wings.
I popped the front grill back into place so I did not have a repeat of the whole sticking a ratchet through the radiator performance.
All in all though things are still heading in the right direction. There is still other work to be completed while I save for a turbo but I was hoping to have it on the road in about a month. Hey ho things can always be worse eh.
Christmas time is once again upon us! It seems to come around quicker and quicker each year. My home seems to resemble Santa’s grotto more as each passes but I don’t mind that at all.
I would just like to Wish all of you out there a very Merry Christmas! May you all have the best one you can and remember it’s not about what you get given but trying to enjoy time with Family and close friends, then congratulating yourself at the end of the day when they have all left without you killing them…
Merry Christmas All 🙂